QUEST update
Gabriel Gonzalez
gabrielg74 at juarez.chih.cablemas.com
Mon Jul 28 10:29:17 AKDT 2003
Thank you very much, I really appreciate it.
One more request, would you have pictures of your setup (engine and tank setup)?
Thanks again,
Gabriel
----- Original Message -----
From: Henderson,Eric
To: discussion at nsrca.org
Sent: Monday, July 28, 2003 11:31 AM
Subject: RE: QUEST update
No engine but I'll fwd my posts directly to you.
-----Original Message-----
From: discussion-request at nsrca.org [mailto:discussion-request at nsrca.org]On Behalf Of Gabriel Gonzalez
Sent: Monday, July 28, 2003 1:31 PM
To: discussion at nsrca.org
Subject: Re: QUEST update
Hi Eric,
Is there a search engine for this mailing list?
I'd like to get the previous info for the Quest, as I am building mine, and would like to get all the info I can.
Thanks,
Gabriel
----- Original Message -----
From: Henderson,Eric
To: discussion at nsrca.org
Sent: Sunday, July 27, 2003 8:16 AM
Subject: RE: QUEST update
Sent you all the back-issue - enjoy!
-----Original Message-----
From: discussion-request at nsrca.org [mailto:discussion-request at nsrca.org]On Behalf Of heli4me at sbcglobal.net
Sent: Saturday, July 26, 2003 11:14 PM
To: discussion at nsrca.org
Subject: Re: QUEST update
Eric I have been late on this thread, is this the Guest .90 from creek hobbies you are talking about?
Send me your e-mail so I can talk to you off list
Thanks.............JOHN
----- Original Message -----
From: Henderson,Eric
To: discussion at nsrca.org
Sent: Saturday, July 26, 2003 10:07 PM
Subject: QUEST update
The Quest continues to be put through the wringer!
With 38 more flights on it I have only had to tighten the tailwheel wire in the rudder. A few drops of Zap did the trick.
The throttle hook up has not been very well behaved. Against my better judgement I used an EZ connector at the throttle arm end. The first failure was on the ground, while tethered. Full rpm on engine start. Saved the day by backing out the needle until the engine quit. The black keeper washer had come off. Fitted a new one. 12 flights later the darn thing came off in the air. The brass part must have also been worn,
11 minutes of full bore flying later it ran out of gas.
All I could do was fly large horizontal figure 8's until tank empty status occurred. Boy does that tire you out! You dare not gain height nor can you roll much at that speed.
Good news is that the plane held together at a faster than I would ever fly it speed. Two bits of trim began to peel but will be re-ironed tonight. Wing and fuse and elevator/ rudder all behaved flawlessly during the un-planned "stress-test". Pilot was not so firm afterwards.
Throttle wire hook up will be replaced with my own system tomorrow.
I am currently flying the plane with all controls 40% below the minimum recommended and it will roll and snap and spin in a very happy manner, No KE or down line mixes have been found to be necessary. One cool thing is that the plane will do real square KE loops. On the down line you go to full rudder and blip the gas and there you are flying level. To much fun for one guy!
Regards,
Eric.
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